Difference between revisions of "Scampi"
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Line 32: | Line 32: | ||
*Results: | *Results: | ||
**Bracket Style: | **Bracket Style: | ||
− | ***[(Video Link) ( | + | ***[(Video Link) loss vs Nasti] |
+ | ***[(Video Link) loss vs Tailspin] | ||
+ | |||
****(notes) | ****(notes) | ||
****(observations)) | ****(observations)) | ||
Line 45: | Line 47: | ||
|- | |- | ||
| Drive Motors | | Drive Motors | ||
− | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;"> | + | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;">22mm BotKits Gear Motor</span><br/> |
|- | |- | ||
| Drive Motor Controllers | | Drive Motor Controllers | ||
− | | | + | | Scorpion |
|- | |- | ||
| Weapon Motor | | Weapon Motor | ||
− | | | + | | PROPDRIVE v2 2830 800KV Brushless Outrunner Motor |
|- | |- | ||
| Weapon Motor Controllers | | Weapon Motor Controllers | ||
− | | | + | | Unknown, ordered a cobra but it didn't work for us |
|- | |- | ||
| Receiver | | Receiver | ||
Line 70: | Line 72: | ||
|- | |- | ||
| Max Weapon RPM | | Max Weapon RPM | ||
− | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;"> | + | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;">1200 RPM</span><br/> |
|- | |- | ||
| Min Spin Up Time | | Min Spin Up Time | ||
− | | | + | | 4 seconds |
|- | |- | ||
| Drive Speed | | Drive Speed | ||
− | | | + | | 4 ft/s |
|} | |} | ||
==== Problems ==== | ==== Problems ==== | ||
− | * | + | *When damaged, the shaft has much more rotational friction, so the weapon struggles to spin up after a hit. |
− | * | + | *Replaced back plate with plastic for weight, battery fell out in every match because the back plate broke or came off. |
− | * | + | *Slight skew to the right when driving forwards |
− | *( | + | *None relevant to match, some ESCs exploded before competition. (not our fault) |
==== Good aspects ==== | ==== Good aspects ==== | ||
− | * | + | *Weapon hit a robot across 10ft arena, was very hype. |
− | * | + | *Wheels coated in latex, helped probably |
− | * | + | *Did not explode in match |
− | |||
==== Changes/Improvements ==== | ==== Changes/Improvements ==== | ||
− | * | + | *Switched from a modular design to a vertical spinner because our robot was 3.5 lbs in the 3lb category. |
− | * | + | *Latex wheels |
− | + | ||
− | |||
== Gallery == | == Gallery == |
Revision as of 19:16, 21 April 2023
(Bot Name) | |
---|---|
Year Of Creation | 20XX-20XX |
Wins/Losses | X/X |
Information and Statistics | |
Weight Class | BeetleWeight |
Weapon Class | (weapon type) |
Combined Wins/Losses | X/X |
(Replace this text with an overall introduction of your robot's design, name, features, ect)
Contents
Competitions
State of Franklin Robot Rumble 2023
- Results:
- Bracket Style:
- [(Video Link) loss vs Nasti]
- [(Video Link) loss vs Tailspin]
- Bracket Style:
- (notes)
- (observations))
Version
(Bot Name) VX.X
Created by: (Names of Builders/Group Members of aforementioned version of bot)
Drive Motors | 22mm BotKits Gear Motor |
Drive Motor Controllers | Scorpion |
Weapon Motor | PROPDRIVE v2 2830 800KV Brushless Outrunner Motor |
Weapon Motor Controllers | Unknown, ordered a cobra but it didn't work for us |
Receiver | Hobby King 2.4Ghz Receiver 6Ch V2 |
Remote Control | Hobby King 2.4Ghz 6Ch Tx and Rx V2 |
Battery | MaxAmps 3s 1050mah |
Max Weapon RPM | 1200 RPM |
Min Spin Up Time | 4 seconds |
Drive Speed | 4 ft/s |
Problems
- When damaged, the shaft has much more rotational friction, so the weapon struggles to spin up after a hit.
- Replaced back plate with plastic for weight, battery fell out in every match because the back plate broke or came off.
- Slight skew to the right when driving forwards
- None relevant to match, some ESCs exploded before competition. (not our fault)
Good aspects
- Weapon hit a robot across 10ft arena, was very hype.
- Wheels coated in latex, helped probably
- Did not explode in match
Changes/Improvements
- Switched from a modular design to a vertical spinner because our robot was 3.5 lbs in the 3lb category.
- Latex wheels
Gallery
- (whatever images and videos you have)
Notes:
(random joke, optional)
(Naming inspiration, optional)
(Names of original builders)