Difference between revisions of "(un)Lucki"
Athrasher7 (talk | contribs) (→Good aspects) |
Athrasher7 (talk | contribs) (→Problems) |
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*(List of Problems, 1 per bullet point) | *(List of Problems, 1 per bullet point) | ||
− | - Our belt was too tight around the motor and weapon, which may have been the cause of the weapon failing to spin up on occasion. | + | - Our belt was too tight around the motor and weapon, which may have been the cause of the weapon failing to spin up on occasion. |
+ | |||
+ | - Putting together our weapon assembly was time consuming and difficult | ||
+ | |||
- Screws shearing due to a drum spinner which gave hits to our bottom plate | - Screws shearing due to a drum spinner which gave hits to our bottom plate | ||
+ | |||
- Wiring packing would bump up against our drive motors and cause them to lock up, even after zip tying | - Wiring packing would bump up against our drive motors and cause them to lock up, even after zip tying | ||
+ | |||
- Weapon deformation after hit, which destroyed our bearing and made us unable to spin up | - Weapon deformation after hit, which destroyed our bearing and made us unable to spin up | ||
+ | |||
- Driving on skids was difficult | - Driving on skids was difficult | ||
+ | |||
- The gearboxes started falling apart | - The gearboxes started falling apart | ||
+ | |||
- ESCs were malfunctioning | - ESCs were malfunctioning | ||
+ | |||
- it catcheded on fire | - it catcheded on fire | ||
Revision as of 18:30, 22 February 2019
(un)Lucki | |
---|---|
Year Of Creation | 2018-2019 |
Versions | |
Current Version | 1.0 |
Wins/Losses | 0/2 |
Information and Statistics | |
Weight Class | BeetleWeight |
Weapon Class | Vertical Bar Spinner |
Combined Wins/Losses | 0/2 |
(Replace this text with an overall introduction of your robot's design, name, features, ect)
Contents
Competitions
Motorama 2019
- Results: 0/2
- Bracket Style: Double Elimination
- [(Video Link) (result) vs (opponent)]
- (notes)
- (observations))
- [(Video Link) (result) vs (opponent)]
- (notes)
- (observations))
- [(Video Link) (result) vs (opponent)]
- Bracket Style: Double Elimination
Versions
(un)Lucki
Created by: (Names of Builders/Group Members of aforementioned version of bot)
Drive Motors | DYS BE1806 2300KV Motors |
Drive Motor Gearboxes | KITBOTS 1000rpm Gearmotor Gearboxes |
Drive Motor Controllers | DYS 20A Micro Opto Multi-rotor ESC |
Weapon Motor | (Weapon Motor Name) |
Weapon Motor Controllers | (Weapon Motor Controller Name) |
Receiver | Turnigy T6A-V2 AFHDS 2.4GHz 6Ch Receiver V2 |
Remote Control | Turnigy T6A-V2 AFHDS 2.4GHz 6Ch Transmitter V2 |
Battery | Turnigy Nano-Tech 1000mAh 3s 45~90c LiPo Pack |
Problems
- (List of Problems, 1 per bullet point)
- Our belt was too tight around the motor and weapon, which may have been the cause of the weapon failing to spin up on occasion.
- Putting together our weapon assembly was time consuming and difficult
- Screws shearing due to a drum spinner which gave hits to our bottom plate
- Wiring packing would bump up against our drive motors and cause them to lock up, even after zip tying
- Weapon deformation after hit, which destroyed our bearing and made us unable to spin up
- Driving on skids was difficult
- The gearboxes started falling apart
- ESCs were malfunctioning
- it catcheded on fire
Good aspects
- (List of good aspects, 1 per bullet point)
- Our bot was invertable due to our fins - The armor held up well under hard hits and pressure - The wedges held up surprisingly well
Changes/Improvements
- (List of suggested improvements/changes, 1 per bullet point)
Notes:
(random joke, optional)
(Naming inspiration, optional)
(Names of original builders)