Difference between revisions of "Robocup 2018 Fleet"

From RoboJackets Wiki
Jump to navigation Jump to search
(Add more things)
 
(4 intermediate revisions by 2 users not shown)
Line 8: Line 8:
 
= Competitions =
 
= Competitions =
  
=== [[Robocup 2018]] ===
+
=== Robocup 2018 ===
 
*Results
 
*Results
 
** Loss vs. Neu Islanders
 
** Loss vs. Neu Islanders
Line 17: Line 17:
 
** Loss vs. UBC Thunderbots
 
** Loss vs. UBC Thunderbots
  
= Good Aspects =
+
= Good aspects from competition =
* Significantly more mechanically consistent than previous iterations
+
* Wheels rolled pretty consistently and did not slip on the carpet terribly often
 +
* Kicks were very consistent, and the kicker did not break
 +
* Shell design was user-friendly, and robust
 +
* Batteries were extremely long lasting
 +
* Control boards were extremely robust
  
= Problems =
+
= Issues at competition =
* No Chipper
+
* Lack of chipper made strategy much harder
* Foam dribblers disintegrated slowly while dribbling
+
* Dribbler material was not appropriate
* Dribbler didn't damp incoming balls very well, especially after the foam was damaged
+
** Using foam is not acceptable compared to a plastic or rubber material
 +
** The dampening aspect of the dribbler is not as important as the grippiness for the dribbler roller
 
* MBed is incapable of doing enough floating point calculations to process IMU inputs for motion control
 
* MBed is incapable of doing enough floating point calculations to process IMU inputs for motion control
 
* The Decawave radios cut out when the referee walks in between them
 
* The Decawave radios cut out when the referee walks in between them
 +
* Capture did not work
  
= Changes/Improvements =
+
= Changes/Improvements for 2019 Fleet =
* Develop a chipper
+
* Develop a chipper to facilitate starts
* Add mechanical damping to the dribbler
+
* Add damping to the dribbler to facilitate passing
* Creating a custom version of the MBed based on the Cortex-M7
+
* Build upon the usability of the previous shell, and make it semi-permanent
 +
* Build upon the wheels to make a smoother ride
 +
* Create a custom version of the MBed based on the Cortex-M7
 
* Consider other radio options
 
* Consider other radio options
 +
* Rebuild capture play to enable passing
 +
 +
[[Category: RoboCup]]

Latest revision as of 19:47, 22 May 2020

Robocup 2018 Robot
480x480px[[File:]]

Competitions

Robocup 2018

  • Results
    • Loss vs. Neu Islanders
    • Tie vs. ULtron
    • Win vs. AMC
    • Tie vs. RoboIME
    • Win vs. RoboFEI
    • Loss vs. UBC Thunderbots

Good aspects from competition

  • Wheels rolled pretty consistently and did not slip on the carpet terribly often
  • Kicks were very consistent, and the kicker did not break
  • Shell design was user-friendly, and robust
  • Batteries were extremely long lasting
  • Control boards were extremely robust

Issues at competition

  • Lack of chipper made strategy much harder
  • Dribbler material was not appropriate
    • Using foam is not acceptable compared to a plastic or rubber material
    • The dampening aspect of the dribbler is not as important as the grippiness for the dribbler roller
  • MBed is incapable of doing enough floating point calculations to process IMU inputs for motion control
  • The Decawave radios cut out when the referee walks in between them
  • Capture did not work

Changes/Improvements for 2019 Fleet

  • Develop a chipper to facilitate starts
  • Add damping to the dribbler to facilitate passing
  • Build upon the usability of the previous shell, and make it semi-permanent
  • Build upon the wheels to make a smoother ride
  • Create a custom version of the MBed based on the Cortex-M7
  • Consider other radio options
  • Rebuild capture play to enable passing