Difference between revisions of "360i"

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(360i V1.0)
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! scope="row" style="text-align:left" | Update Year
 
! scope="row" style="text-align:left" | Update Year
| {{{updyr|20XX-20XX}}}
+
| {{{updyr|2025}}}
 
|-
 
|-
 
! scope="row" style="text-align:left" | Wins/Losses
 
! scope="row" style="text-align:left" | Wins/Losses
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|}
 
|}
  
(basic summary of robot)
+
3lb Full Body Shell Spinner composed mainly of TPU, with a mix of Carbon Fiber-Nylon and G10 inserts for rigidity. Impactors are made of steel, and
  
 
== Competitions ==
 
== Competitions ==
  
=== [[Motorama_20XX|Motorama 20XX]] ===
+
=== [[UGA_Spring_Smash_2025|UGA Spring Smash 2025]] ===
  
*Results:
+
*Results: 0-2
**Bracket Style:
+
**Bracket Style: Double Elimination
***[(Video Link) (result) vs (opponent)]
+
***[https://youtu.be/OXjSGaipxs0?t=7553 TO Loss vs Panzer]
****(notes)
+
****Snapping of the self righting bar 1 minute into the match led to getting stuck
****(observations))
+
****Early tap out (it was really dramatic)
  
 +
***[https://youtu.be/OXjSGaipxs0?t=18701 JD Loss vs Intern Mousse]
 +
****Weaker Drive motors lead to getting out controlled
 +
****Slow spin up time and low max spin-up speed lead
 +
**** For all practical purposes, they had an active weapon while we did not.
 
== Version ==
 
== Version ==
  
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|-
 
|-
 
| Drive Motors
 
| Drive Motors
| <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;">(DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors
+
| <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;">DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors
  
 
)</span><br/>
 
)</span><br/>
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|-
 
|-
 
| Battery
 
| Battery
| (Battery Name)
+
| 3S 930 mAh Gaoeng Power LiPo Light (The Flower One)
 
|-
 
|-
 
| (OTHER:)
 
| (OTHER:)
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- Insufficient Contact Between the Motor and the Shell
 
- Insufficient Contact Between the Motor and the Shell
- Tolerancing Issues --> From CAD to Bot
+
- Tolerancing Issues in desin
 
- Not enough Torque in our motor to spin the shell up
 
- Not enough Torque in our motor to spin the shell up
- Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process
+
- Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process. Printing Out the Shell took forever.
 
+
- Terrible file management lead to a delay in 3 weeks in manufacturing.
 
==== Good aspects ====
 
==== Good aspects ====
  
 
- Chassis worked great + drive was smooth
 
- Chassis worked great + drive was smooth
 
- Nylon-Ring Inserts reduced deformation caused from spinning
 
- Nylon-Ring Inserts reduced deformation caused from spinning
- G10 Instead of Nylon-Carbon Fiber  
+
- G10 Instead of Nylon-Carbon Fiber helped with manufacturability
 
==== Changes/Improvements ====
 
==== Changes/Improvements ====
  
*(List of suggested improvements/changes, 1 per bullet point)
+
- Larger driving wheel and larger motor for torque issues
 
+
- Clear and effective file management
 
== See also ==
 
== See also ==
 
<ul style="line-height: 20.7999992370605px;">
 
<ul style="line-height: 20.7999992370605px;">

Revision as of 20:02, 25 April 2025

360i
Year Of Creation 2024-2025
Versions
Current Version 1.0
Update Year 2025
Wins/Losses 0/2
Information and Statistics
Weight Class BeetleWeight
Weapon Class (Full Body Shell Spinner)
Combined Wins/Losses 0/2
Weapon Speed (Theoretical --> 11000 rpm
("Temporary") ("Temporary")

3lb Full Body Shell Spinner composed mainly of TPU, with a mix of Carbon Fiber-Nylon and G10 inserts for rigidity. Impactors are made of steel, and

Competitions

UGA Spring Smash 2025

  • Results: 0-2
    • Bracket Style: Double Elimination
      • TO Loss vs Panzer
        • Snapping of the self righting bar 1 minute into the match led to getting stuck
        • Early tap out (it was really dramatic)
      • JD Loss vs Intern Mousse
        • Weaker Drive motors lead to getting out controlled
        • Slow spin up time and low max spin-up speed lead
        • For all practical purposes, they had an active weapon while we did not.

Version

360i V1.0

Created by: Shri Thada and help (look at the bottom of the page)

Drive Motors DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors

)

Drive Motor Controllers Repeat Beetle Brushed DESC 2x15A
Weapon Motor BadAss 2814-1120Kv Brushless Motor
Weapon Motor Controllers Pariah 70A AM32 ESC
Receiver Hobby King 2.4Ghz Receiver 6Ch V2
Remote Control Flysky TMXX FS-TMXX 2.4G V2
Battery 3S 930 mAh Gaoeng Power LiPo Light (The Flower One)
(OTHER:)

Problems

- Insufficient Contact Between the Motor and the Shell - Tolerancing Issues in desin - Not enough Torque in our motor to spin the shell up - Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process. Printing Out the Shell took forever. - Terrible file management lead to a delay in 3 weeks in manufacturing.

Good aspects

- Chassis worked great + drive was smooth - Nylon-Ring Inserts reduced deformation caused from spinning - G10 Instead of Nylon-Carbon Fiber helped with manufacturability

Changes/Improvements

- Larger driving wheel and larger motor for torque issues - Clear and effective file management

See also

  • [(link to other bot made this year) (Name of other bot made this year)]

Notes:

(random joke, optional)

Naming Inspiration: https://www.youtube.com/watch?v=WJW-VvmRKsE

Names of original builders: Aaron Qu, Aleck Sun, Brooklyn Heath, Deep Patel, Emilio Revelo, Ian Lamont, Isabel A, Justin Senh, Muhammad Moazzam Salman, Nathan Griskenas, Yara Khan, Zaid Hashmi

(Mentor: Angelina Rodriguez, Step Mentor: Dylan Park, The Goat: Shri, Shell Idea Master: Martha)