Difference between revisions of "360i"
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! scope="row" colspan="2" style="background-color:#FFFF99" | 360i | ! scope="row" colspan="2" style="background-color:#FFFF99" | 360i | ||
|- | |- | ||
− | ! scope="row" colspan="2" | [[File: | + | ! scope="row" colspan="2" | [[File:Shelllol.jpg|frameless|right|480x360px|(Highlight text)]] |
|- | |- | ||
! scope="row" style="text-align:left" | Year Of Creation | ! scope="row" style="text-align:left" | Year Of Creation | ||
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|- | |- | ||
! scope="row" style="text-align:left" | Update Year | ! scope="row" style="text-align:left" | Update Year | ||
− | | {{{updyr| | + | | {{{updyr|2025}}} |
|- | |- | ||
! scope="row" style="text-align:left" | Wins/Losses | ! scope="row" style="text-align:left" | Wins/Losses | ||
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|- | |- | ||
! scope="row" style="text-align:left" | Weapon Class | ! scope="row" style="text-align:left" | Weapon Class | ||
− | | {{{weapc| | + | | {{{weapc|Full Body Shell Spinner}}} |
|- | |- | ||
! scope="row" style="text-align:left" | Combined Wins/Losses | ! scope="row" style="text-align:left" | Combined Wins/Losses | ||
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|- | |- | ||
! scope="row" style="text-align:left" | Weapon Speed | ! scope="row" style="text-align:left" | Weapon Speed | ||
− | | {{{TBA| | + | | {{{TBA|Theoretical --> 11000 rpm| Actual --> 3600 rpm (MAX)}}} |
|- | |- | ||
! scope="row" style="text-align:left" | ("Temporary") | ! scope="row" style="text-align:left" | ("Temporary") | ||
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|} | |} | ||
− | + | 3lb Full Body Shell Spinner composed mainly of TPU, with a mix of Carbon Fiber-Nylon and G10 inserts for rigidity. Impactors are made of steel, and | |
== Competitions == | == Competitions == | ||
− | === [[ | + | === [[UGA_Spring_Smash_2025|UGA Spring Smash 2025]] === |
− | *Results: | + | *Results: 0-2 |
− | **Bracket Style: | + | **Bracket Style: Double Elimination |
− | ***[ | + | ***[https://youtu.be/OXjSGaipxs0?t=7553 TO Loss vs Panzer] |
− | **** | + | ****Snapping of the self righting bar 1 minute into the match led to getting stuck |
− | ****( | + | ****Early tap out (it was really dramatic) |
+ | ***[https://youtu.be/OXjSGaipxs0?t=18701 JD Loss vs Intern Mousse] | ||
+ | ****Weaker Drive motors lead to getting out controlled | ||
+ | ****Slow spin up time and low max spin-up speed lead | ||
+ | **** For all practical purposes, they had an active weapon while we did not. | ||
== Version == | == Version == | ||
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|- | |- | ||
| Drive Motors | | Drive Motors | ||
− | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;"> | + | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;">DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors |
)</span><br/> | )</span><br/> | ||
Line 78: | Line 82: | ||
|- | |- | ||
| Battery | | Battery | ||
− | | ( | + | | 3S 930 mAh Gaoeng Power LiPo Light (The Flower One) |
|- | |- | ||
| (OTHER:) | | (OTHER:) | ||
Line 86: | Line 90: | ||
==== Problems ==== | ==== Problems ==== | ||
− | + | *Insufficient Contact Between the Motor and the Shell | |
− | + | *Tolerancing Issues in desin | |
− | + | *Not enough Torque in our motor to spin the shell up | |
− | + | *Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process. Printing Out the Shell took forever. | |
+ | *Terrible file management lead to a delay in 3 weeks in manufacturing. | ||
==== Good aspects ==== | ==== Good aspects ==== | ||
− | + | *Chassis worked great + drive was smooth | |
− | + | *Nylon-Ring Inserts reduced deformation caused from spinning | |
− | + | *G10 Instead of Nylon-Carbon Fiber helped with manufacturability | |
+ | |||
==== Changes/Improvements ==== | ==== Changes/Improvements ==== | ||
− | * | + | *Larger driving wheel and larger motor for torque issues |
+ | *Clear and effective file management | ||
== See also == | == See also == | ||
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<span style="line-height: 20.7999992370605px">Names of original builders: Aaron Qu, Aleck Sun, Brooklyn Heath, Deep Patel, Emilio Revelo, Ian Lamont, Isabel A, Justin Senh, Muhammad Moazzam Salman, Nathan Griskenas, Yara Khan, Zaid Hashmi</span> | <span style="line-height: 20.7999992370605px">Names of original builders: Aaron Qu, Aleck Sun, Brooklyn Heath, Deep Patel, Emilio Revelo, Ian Lamont, Isabel A, Justin Senh, Muhammad Moazzam Salman, Nathan Griskenas, Yara Khan, Zaid Hashmi</span> | ||
− | <span style="line-height: 20.7999992370605px"> | + | <span style="line-height: 20.7999992370605px">Mentor: Angelina Rodriguez, Step Mentor: Dylan Park, The Goat: Shri, Shell Idea Master: Martha</span> |
[[Category:BattleBots]] [[Category:BeetleWeights]][[Category:Template documentation pages]] | [[Category:BattleBots]] [[Category:BeetleWeights]][[Category:Template documentation pages]] |
Latest revision as of 20:38, 25 April 2025
360i | |
---|---|
Year Of Creation | 2024-2025 |
Versions | |
Current Version | 1.0 |
Update Year | 2025 |
Wins/Losses | 0/2 |
Information and Statistics | |
Weight Class | BeetleWeight |
Weapon Class | Full Body Shell Spinner |
Combined Wins/Losses | 0/2 |
Weapon Speed | Theoretical --> 11000 rpm |
("Temporary") | ("Temporary") |
3lb Full Body Shell Spinner composed mainly of TPU, with a mix of Carbon Fiber-Nylon and G10 inserts for rigidity. Impactors are made of steel, and
Contents
Competitions
UGA Spring Smash 2025
- Results: 0-2
- Bracket Style: Double Elimination
- TO Loss vs Panzer
- Snapping of the self righting bar 1 minute into the match led to getting stuck
- Early tap out (it was really dramatic)
- TO Loss vs Panzer
- Bracket Style: Double Elimination
- JD Loss vs Intern Mousse
- Weaker Drive motors lead to getting out controlled
- Slow spin up time and low max spin-up speed lead
- For all practical purposes, they had an active weapon while we did not.
- JD Loss vs Intern Mousse
Version
360i V1.0
Created by: Shri Thada and help (look at the bottom of the page)
Drive Motors | DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors
) |
Drive Motor Controllers | Repeat Beetle Brushed DESC 2x15A |
Weapon Motor | BadAss 2814-1120Kv Brushless Motor |
Weapon Motor Controllers | Pariah 70A AM32 ESC |
Receiver | Hobby King 2.4Ghz Receiver 6Ch V2 |
Remote Control | Flysky TMXX FS-TMXX 2.4G V2 |
Battery | 3S 930 mAh Gaoeng Power LiPo Light (The Flower One) |
(OTHER:) |
Problems
- Insufficient Contact Between the Motor and the Shell
- Tolerancing Issues in desin
- Not enough Torque in our motor to spin the shell up
- Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process. Printing Out the Shell took forever.
- Terrible file management lead to a delay in 3 weeks in manufacturing.
Good aspects
- Chassis worked great + drive was smooth
- Nylon-Ring Inserts reduced deformation caused from spinning
- G10 Instead of Nylon-Carbon Fiber helped with manufacturability
Changes/Improvements
- Larger driving wheel and larger motor for torque issues
- Clear and effective file management
See also
- [(link to other bot made this year) (Name of other bot made this year)]
Notes:
(random joke, optional)
Naming Inspiration: https://www.youtube.com/watch?v=WJW-VvmRKsE
Names of original builders: Aaron Qu, Aleck Sun, Brooklyn Heath, Deep Patel, Emilio Revelo, Ian Lamont, Isabel A, Justin Senh, Muhammad Moazzam Salman, Nathan Griskenas, Yara Khan, Zaid Hashmi
Mentor: Angelina Rodriguez, Step Mentor: Dylan Park, The Goat: Shri, Shell Idea Master: Martha