Difference between revisions of "Loki"
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{| class="wikitable" align="right" | {| class="wikitable" align="right" | ||
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− | ! scope="row" colspan="2" style="background-color:#FFFF99" | | + | ! scope="row" colspan="2" style="background-color:#FFFF99" | Loki |
|- | |- | ||
! scope="row" colspan="2" | [[File:(Image filename)|frameless|right|480x360px|(Highlight text)]] | ! scope="row" colspan="2" | [[File:(Image filename)|frameless|right|480x360px|(Highlight text)]] | ||
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! scope="row" style="text-align:left" | Current Version | ! scope="row" style="text-align:left" | Current Version | ||
− | | | + | | 1.0 |
|- | |- | ||
! scope="row" style="text-align:left" | Update Year | ! scope="row" style="text-align:left" | Update Year | ||
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|- | |- | ||
! scope="row" style="text-align:left" | Weapon Class | ! scope="row" style="text-align:left" | Weapon Class | ||
− | | | + | | Horizontal Bar Spinner |
|- | |- | ||
! scope="row" style="text-align:left" | Combined Wins/Losses | ! scope="row" style="text-align:left" | Combined Wins/Losses | ||
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|- | |- | ||
! scope="row" style="text-align:left" | Weapon Speed | ! scope="row" style="text-align:left" | Weapon Speed | ||
− | | | + | | ??? |
|- | |- | ||
! scope="row" style="text-align:left" | ("Temporary") | ! scope="row" style="text-align:left" | ("Temporary") | ||
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− | + | Loki 1.0 is a 3 - pound horizontal bar spinner featuring a plastic chassis milled from a single block of UHMW high-density polyethylene, a powerful 6 - cell motor, and an extremely large weapon relative to the size of the chassis. Very much a "the best offense is a good defense" robot, Loki 1.0 lacked significant armor protecting vital components. Whether this would have been detrimental in a battle will never be known, as Loki 1.0 was working in time to compete in its first match against Silent Spring at Motorama 2018, and its drive motors were removed to supplement the failing drive motors that plagued other robots. | |
== Competitions == | == Competitions == | ||
− | === [[ | + | === [[Motorama_2018|Motorama 2018]] === |
*Results: | *Results: | ||
**Bracket Style: | **Bracket Style: | ||
− | ***[ | + | ***Forfeit vs. Silent Spring [No Video] |
− | **** | + | ****Was not working in time to compete |
− | **** | + | ****Avoided getting completely wrecked |
+ | ***Forfeit vs. Disko 3 [No Video] | ||
+ | ****Was not magically finished in the 15 minutes between matches | ||
== Version == | == Version == | ||
− | === | + | === Loki V1.0 === |
− | Created by: | + | Created by: Eli Tiemann, C. Quinn Johnson, Benjamin Iglesia |
{| border="1" cellspacing="1" cellpadding="1" style="width: 500px;" | {| border="1" cellspacing="1" cellpadding="1" style="width: 500px;" | ||
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|- | |- | ||
| Weapon Motor | | Weapon Motor | ||
− | | | + | | Quanum MT Series 4108 700KV Brushless Multirotor Motor |
|- | |- | ||
| Weapon Motor Controllers | | Weapon Motor Controllers | ||
Line 84: | Line 86: | ||
==== Problems ==== | ==== Problems ==== | ||
− | * | + | *Did not have enough room inside for wires, causing the bottom plate to stick out further than designed. |
+ | *Screw holes on the bottom plate were not properly aligned with the holes on the chassis. This, coupled with the aforementioned point, caused numerous other parts to become misaligned, and contributed significantly to Loki's inability to compete at Motorama 2018. | ||
==== Good aspects ==== | ==== Good aspects ==== | ||
− | * | + | *6 - cell motor and battery was extremely powerful. |
+ | *UHMW HDPE chassis was lightweight and strong. | ||
==== Changes/Improvements ==== | ==== Changes/Improvements ==== | ||
− | * | + | *Make internal cavity much larger to allow more space for wiring. |
+ | *Add protective guards for wheels and pulleys. | ||
== See also == | == See also == | ||
Line 101: | Line 106: | ||
== Notes: == | == Notes: == | ||
− | + | Loki technically never lost a match. | |
− | + | (Random Joke) | |
− | + | Named for the Norse trickster god. Low key a pretty good name. | |
− | [[Category:BattleBots]] [[Category:BeetleWeights]] | + | |
+ | Original Builders: Eli Tiemann, C. Quinn Johnson, Benjamin Iglesia | ||
+ | [[Category:BattleBots]] [[Category:BeetleWeights]][[Category:2017-2018]] |
Latest revision as of 18:31, 29 August 2023
Loki | |
---|---|
Year Of Creation | 20XX-20XX |
Versions | |
Current Version | 1.0 |
Update Year | 20XX-20XX |
Wins/Losses | X/X |
Information and Statistics | |
Weight Class | BeetleWeight |
Weapon Class | Horizontal Bar Spinner |
Combined Wins/Losses | X/X |
Weapon Speed | ??? |
("Temporary") | ("Temporary") |
Loki 1.0 is a 3 - pound horizontal bar spinner featuring a plastic chassis milled from a single block of UHMW high-density polyethylene, a powerful 6 - cell motor, and an extremely large weapon relative to the size of the chassis. Very much a "the best offense is a good defense" robot, Loki 1.0 lacked significant armor protecting vital components. Whether this would have been detrimental in a battle will never be known, as Loki 1.0 was working in time to compete in its first match against Silent Spring at Motorama 2018, and its drive motors were removed to supplement the failing drive motors that plagued other robots.
Contents
Competitions
Motorama 2018
- Results:
- Bracket Style:
- Forfeit vs. Silent Spring [No Video]
- Was not working in time to compete
- Avoided getting completely wrecked
- Forfeit vs. Disko 3 [No Video]
- Was not magically finished in the 15 minutes between matches
- Forfeit vs. Silent Spring [No Video]
- Bracket Style:
Version
Loki V1.0
Created by: Eli Tiemann, C. Quinn Johnson, Benjamin Iglesia
Drive Motors | (Drive Motor Name) |
Drive Motor Controllers | (Drive Motor Controller Name) |
Weapon Motor | Quanum MT Series 4108 700KV Brushless Multirotor Motor |
Weapon Motor Controllers | (Weapon Motor Controller Name) |
Receiver | Hobby King 2.4Ghz Receiver 6Ch V2 |
Remote Control | Hobby King 2.4Ghz 6Ch Tx and Rx V2 |
Battery | (Battery Name) |
(OTHER:) |
Problems
- Did not have enough room inside for wires, causing the bottom plate to stick out further than designed.
- Screw holes on the bottom plate were not properly aligned with the holes on the chassis. This, coupled with the aforementioned point, caused numerous other parts to become misaligned, and contributed significantly to Loki's inability to compete at Motorama 2018.
Good aspects
- 6 - cell motor and battery was extremely powerful.
- UHMW HDPE chassis was lightweight and strong.
Changes/Improvements
- Make internal cavity much larger to allow more space for wiring.
- Add protective guards for wheels and pulleys.
See also
- [(link to other bot made this year) (Name of other bot made this year)]
Notes:
Loki technically never lost a match.
(Random Joke)
Named for the Norse trickster god. Low key a pretty good name.
Original Builders: Eli Tiemann, C. Quinn Johnson, Benjamin Iglesia