Difference between revisions of "360i"
(→360i V1.0) |
|||
| Line 14: | Line 14: | ||
|- | |- | ||
! scope="row" style="text-align:left" | Update Year | ! scope="row" style="text-align:left" | Update Year | ||
| − | | {{{updyr| | + | | {{{updyr|2025}}} |
|- | |- | ||
! scope="row" style="text-align:left" | Wins/Losses | ! scope="row" style="text-align:left" | Wins/Losses | ||
| Line 37: | Line 37: | ||
|} | |} | ||
| − | + | 3lb Full Body Shell Spinner composed mainly of TPU, with a mix of Carbon Fiber-Nylon and G10 inserts for rigidity. Impactors are made of steel, and | |
== Competitions == | == Competitions == | ||
| − | === [[ | + | === [[UGA_Spring_Smash_2025|UGA Spring Smash 2025]] === |
| − | *Results: | + | *Results: 0-2 |
| − | **Bracket Style: | + | **Bracket Style: Double Elimination |
| − | ***[ | + | ***[https://youtu.be/OXjSGaipxs0?t=7553 TO Loss vs Panzer] |
| − | **** | + | ****Snapping of the self righting bar 1 minute into the match led to getting stuck |
| − | ****( | + | ****Early tap out (it was really dramatic) |
| + | ***[https://youtu.be/OXjSGaipxs0?t=18701 JD Loss vs Intern Mousse] | ||
| + | ****Weaker Drive motors lead to getting out controlled | ||
| + | ****Slow spin up time and low max spin-up speed lead | ||
| + | **** For all practical purposes, they had an active weapon while we did not. | ||
== Version == | == Version == | ||
| Line 58: | Line 62: | ||
|- | |- | ||
| Drive Motors | | Drive Motors | ||
| − | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;"> | + | | <span style="color: rgb(0, 0, 0); font-family: arial, sans, sans-serif; line-height: normal; white-space: pre-wrap;">DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors |
)</span><br/> | )</span><br/> | ||
| Line 78: | Line 82: | ||
|- | |- | ||
| Battery | | Battery | ||
| − | | ( | + | | 3S 930 mAh Gaoeng Power LiPo Light (The Flower One) |
|- | |- | ||
| (OTHER:) | | (OTHER:) | ||
| Line 87: | Line 91: | ||
- Insufficient Contact Between the Motor and the Shell | - Insufficient Contact Between the Motor and the Shell | ||
| − | - Tolerancing Issues | + | - Tolerancing Issues in desin |
- Not enough Torque in our motor to spin the shell up | - Not enough Torque in our motor to spin the shell up | ||
| − | - Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process | + | - Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process. Printing Out the Shell took forever. |
| − | + | - Terrible file management lead to a delay in 3 weeks in manufacturing. | |
==== Good aspects ==== | ==== Good aspects ==== | ||
- Chassis worked great + drive was smooth | - Chassis worked great + drive was smooth | ||
- Nylon-Ring Inserts reduced deformation caused from spinning | - Nylon-Ring Inserts reduced deformation caused from spinning | ||
| − | - G10 Instead of Nylon-Carbon Fiber | + | - G10 Instead of Nylon-Carbon Fiber helped with manufacturability |
==== Changes/Improvements ==== | ==== Changes/Improvements ==== | ||
| − | + | - Larger driving wheel and larger motor for torque issues | |
| − | + | - Clear and effective file management | |
== See also == | == See also == | ||
<ul style="line-height: 20.7999992370605px;"> | <ul style="line-height: 20.7999992370605px;"> | ||
Revision as of 19:02, 25 April 2025
| 360i | |
|---|---|
| Year Of Creation | 2024-2025 |
| Versions | |
| Current Version | 1.0 |
| Update Year | 2025 |
| Wins/Losses | 0/2 |
| Information and Statistics | |
| Weight Class | BeetleWeight |
| Weapon Class | (Full Body Shell Spinner) |
| Combined Wins/Losses | 0/2 |
| Weapon Speed | (Theoretical --> 11000 rpm |
| ("Temporary") | ("Temporary") |
3lb Full Body Shell Spinner composed mainly of TPU, with a mix of Carbon Fiber-Nylon and G10 inserts for rigidity. Impactors are made of steel, and
Contents
Competitions
UGA Spring Smash 2025
- Results: 0-2
- Bracket Style: Double Elimination
- TO Loss vs Panzer
- Snapping of the self righting bar 1 minute into the match led to getting stuck
- Early tap out (it was really dramatic)
- TO Loss vs Panzer
- Bracket Style: Double Elimination
- JD Loss vs Intern Mousse
- Weaker Drive motors lead to getting out controlled
- Slow spin up time and low max spin-up speed lead
- For all practical purposes, they had an active weapon while we did not.
- JD Loss vs Intern Mousse
Version
360i V1.0
Created by: Shri Thada and help (look at the bottom of the page)
| Drive Motors | DartBox V2 Drive - Lightweight, Ultra Powerful 22mm Gearmotors
) |
| Drive Motor Controllers | Repeat Beetle Brushed DESC 2x15A |
| Weapon Motor | BadAss 2814-1120Kv Brushless Motor |
| Weapon Motor Controllers | Pariah 70A AM32 ESC |
| Receiver | Hobby King 2.4Ghz Receiver 6Ch V2 |
| Remote Control | Flysky TMXX FS-TMXX 2.4G V2 |
| Battery | 3S 930 mAh Gaoeng Power LiPo Light (The Flower One) |
| (OTHER:) |
Problems
- Insufficient Contact Between the Motor and the Shell - Tolerancing Issues in desin - Not enough Torque in our motor to spin the shell up - Utilizing the mark forge to print carbon-fiber nylon is a time intensive and difficult process. Printing Out the Shell took forever. - Terrible file management lead to a delay in 3 weeks in manufacturing.
Good aspects
- Chassis worked great + drive was smooth - Nylon-Ring Inserts reduced deformation caused from spinning - G10 Instead of Nylon-Carbon Fiber helped with manufacturability
Changes/Improvements
- Larger driving wheel and larger motor for torque issues - Clear and effective file management
See also
- [(link to other bot made this year) (Name of other bot made this year)]
Notes:
(random joke, optional)
Naming Inspiration: https://www.youtube.com/watch?v=WJW-VvmRKsE
Names of original builders: Aaron Qu, Aleck Sun, Brooklyn Heath, Deep Patel, Emilio Revelo, Ian Lamont, Isabel A, Justin Senh, Muhammad Moazzam Salman, Nathan Griskenas, Yara Khan, Zaid Hashmi
(Mentor: Angelina Rodriguez, Step Mentor: Dylan Park, The Goat: Shri, Shell Idea Master: Martha)