Difference between revisions of "Tomfooleri"
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== Notes: == | == Notes: == | ||
| − | <span style="line-height: 20.7999992370605px">( | + | <span style="line-height: 20.7999992370605px">Ri1D :P (Robot in 1 Day)</span> |
| − | <span style="line-height: 20.7999992370605px"> | + | <span style="line-height: 20.7999992370605px">Just wanted to make our own plant weight and felt we were getting up to some tomfoolery </span> |
| − | <span style="line-height: 20.7999992370605px"> | + | <span style="line-height: 20.7999992370605px">Ian LaMont and Zaid Hashmi</span> |
[[Category:BattleBots]] [[Category:BeetleWeights]][[Category:Template documentation pages]] | [[Category:BattleBots]] [[Category:BeetleWeights]][[Category:Template documentation pages]] | ||
Revision as of 02:20, 22 April 2025
| (Bot Name) | |
|---|---|
| Year Of Creation | 20XX-20XX |
| Versions | |
| Current Version | X.X |
| Update Year | 20XX-20XX |
| Wins/Losses | X/X |
| Information and Statistics | |
| Weight Class | Plastic Antweight |
| Weapon Class | (weapon type) |
| Combined Wins/Losses | X/X |
| Weapon Speed | (RPM) |
| ("Temporary") | ("Temporary") |
(basic summary of robot)
Contents
Competitions
UGA Spring Smash 3.0
- Results: 5th Place (2-2)
- Bracket Style: Double Elimination
- Win vs Space Force PN
- Win vs split conclusion
- Loss vs Torbor V2
- Loss vs 180i
- (Tomfooleri was a side project plant weight that was designed a few weeks prior to spring smash 3.0 and was built the night before. Expectations were not high but it ended up coming 5th and winning some fights.)
- (The main takeaways were the lack of bite in the weapon and the lack of room for electronics. Room for the electronics was made with a dermal and a soldering iron. And the weapon was effective mostly out of luck.))
- Bracket Style: Double Elimination
Version
Tomfooleri V1.0
Created by: (Names of Builders/Group Members of aforementioned version of bot)
| Drive Motors | Repeat Mini Brushed Mk2 |
| Drive Motor Controllers | Repeat Budget Ant DESC |
| Weapon Motor | FLASH HOBBY D2822 Brushless Motor 2600KV 2-3S |
| Weapon Motor Controllers | DH 20A 2-4S Waterproof Brushless ESC Electronic Speed Controller with 5.5V/4A BEC and XT60 3.5mm Banana Head Connector for Model Ship RC Boat (20A) |
| Receiver | Hobby King 2.4Ghz Receiver 6Ch V2 |
| Remote Control | Hobby King 2.4Ghz 6Ch Tx and Rx V2 |
| Battery | (3S Lipo wrapped in electrical tape) |
| (OTHER:) |
Problems
- No space for electronics
- Due to electronics bulging out, bot was no longer invertible
- Weapon had little to no bite
- Weapon ESC shut down after running at full throttle
- Prints had low wall count leading to fragility
- Weapon motor press fit failed
- Amazon boat esc worked but was too bulky
Good aspects
- PLA drive wheels using hot glue as traction worked far better than anticipated
- Weapon motor being hot glued into weapon to supplement press fit was effective
- Parts were very easy to replace with spares (frequently damaged parts were modular)
- Passed safety, competed, and won 2 fights!
Changes/Improvements
- Make space for electronics in chassis
- Make drum with more bite instead of weird beater bar
- Put wheels inside chassis to serve as protection
- More walls when printing less infill
- Some kind of wedge or forks
See also
Notes:
Ri1D :P (Robot in 1 Day)
Just wanted to make our own plant weight and felt we were getting up to some tomfoolery
Ian LaMont and Zaid Hashmi