Difference between revisions of "Crispi"
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(→Motorama 2019) |
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Line 36: | Line 36: | ||
*Results: 0/2 | *Results: 0/2 | ||
**Bracket Style: Double Elimination | **Bracket Style: Double Elimination | ||
− | ***[ | + | ***[https://youtu.be/F3RkPferg_4 Loss vs Scratch Attack] |
****Horizontal Bar Spinner | ****Horizontal Bar Spinner | ||
****Drive gave out, weapon stopped spinning, drive stopped moving. Basically it was paralyzed in fear. | ****Drive gave out, weapon stopped spinning, drive stopped moving. Basically it was paralyzed in fear. | ||
− | ***[ | + | ***[https://youtu.be/B6HrSwtRtTY Loss vs Entropi] |
****Beater Bar | ****Beater Bar | ||
****Electronics continued to not work and we took a nasty hit to the taco. | ****Electronics continued to not work and we took a nasty hit to the taco. |
Revision as of 14:36, 26 March 2019
Crispi/Crunchi | |
---|---|
Year Of Creation | 2018-2019 |
Versions | |
Current Version | 1.0 |
Wins/Losses | 0/2 |
Information and Statistics | |
Weight Class | BeetleWeight |
Weapon Class | Drum Spinner |
Combined Wins/Losses | 0/2 |
(Replace this text with an overall introduction of your robot's design, name, features, ect)
Contents
Competitions
Motorama 2019
- Results: 0/2
- Bracket Style: Double Elimination
- Loss vs Scratch Attack
- Horizontal Bar Spinner
- Drive gave out, weapon stopped spinning, drive stopped moving. Basically it was paralyzed in fear.
- Loss vs Entropi
- Beater Bar
- Electronics continued to not work and we took a nasty hit to the taco.
- (observations))
- Loss vs Scratch Attack
- Bracket Style: Double Elimination
Versions
Crispi/Crunchi
Created by: The Dennis Rodney Crawford The Third, Brenden Chance Waits, Hoyean Le, Celina Huang, Damian Huerta, Jonathan William Paul and his infinite wisdom, Sanket Something, Alexander Elliott, Annie Liu, Derrick Mu, Nathan Wang
Drive Motors | DYS BE1806 2300KV Motors |
Drive Motor Gearboxes | KITBOTS 1000rpm Gearmotor Gearboxes |
Drive Motor Controllers | DYS 20A Micro Opto Multi-rotor ESC |
Weapon Motor | Turnigy 2836 Brushless EDF Motor 3200kv |
Weapon Motor Controllers | Turnigy ESC 40 A w/ 5A BEC |
Receiver | Turnigy T6A-V2 AFHDS 2.4GHz 6Ch Receiver V2 |
Remote Control | Turnigy T6A-V2 AFHDS 2.4GHz 6Ch Transmitter V2 |
Battery | Turnigy Nano-Tech 1000mAh 3s 45~90c LiPo Pack |
Problems
- Small amount of room for electronics
- Low drive capability, wheels too far back
- High friction on front skids
Good aspects
- Looks menacing as hell
- Chassis held up extremely well
Changes/Improvements
- Move wheels further up towards center of mass
- Lengthen the plastic back taco towards front in order to allow more room for electronics
- Possibly widen or lengthen chassis, which would allow for a longer weapon if widened as well as more room for electronics
Notes:
(random joke, optional)
(Naming inspiration, optional)
(Names of original builders)