Difference between revisions of "Smitti Werbenjagermanjensen"
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*Make the weapon closer to the ground, and cover more of the robot | *Make the weapon closer to the ground, and cover more of the robot | ||
*Find a better way to hold the robot together | *Find a better way to hold the robot together | ||
+ | |||
+ | == See also == | ||
+ | <ul style="line-height: 20.7999992370605px;"> | ||
+ | <li>[http://wiki.robojackets.org/mediawiki/Smitti Werbenjagermanjensen Smitti Werbenjagermanjensen]</li> | ||
+ | <li>[http://wiki.robojackets.org/mediawiki/Emmi Emmi]</li> | ||
+ | <li>[http://wiki.robojackets.org/mediawiki/Vicki Vicki]</li> | ||
+ | <li>[http://wiki.robojackets.org/mediawiki/Flippi/MrWedge Flippi/MrWedge]</li> | ||
+ | <li>[http://wiki.robojackets.org/mediawiki/Group 5 Group 5]</li> | ||
+ | </ul> | ||
== Notes: == | == Notes: == |
Revision as of 20:17, 12 March 2015
Smitti Werbenjagermanjensen | |
---|---|
Year Of Creation | 2014-2015 |
Versions | |
Current Version | 1.0 |
Update Year | 2014-2015 |
Information and Statistics | |
Weight Class | BeetleWeight |
Weapon Class | Ring Spinner |
Wins/Losses | 2/2 |
("Temporary") | ("Temporary") |
("Temporary") | ("Temporary") |
Contents
Competitions
Motorama 2015
- Results:
- Bracket Style:
- Loss vs Time Warp
- Weapon wheel was dislodged early in the fight
- One of the wheels slipped off the motor shaft
- Victory vs RMR
- Weapon ring was dislodged due to the force and frequency at which the enemy was attacked
- one of the teeth was broken off by the spinning bar
- Loss vs The Collective
- Dominated for the first 2 minutes, managed to incapacitate one of the three
- The other two teamed up and managed to dislodge the weapon ring and disable one wheel
- Loss vs Time Warp
- Victory in Beetleweight Rumble
- Weapon ring came loose
- Wheels worked throughout
- Offense and defence were well balanced
- Bracket Style:
Version
V1
Created by: Aman More, Cory Stine, and Dustin Sloan
Drive Motors | Pololu 9.7:1 Metal Gearmotor 25Dx48L mm HP |
Drive Motor Controllers | Sabertooth 2X5 Motor Controller 2X5A |
Weapon Motor | Turnigy Multistar 3508-640Kv 14Pole Multi-Rotor Outrunner |
Weapon Motor Controllers | Turnigy Plush 40amp Speed Controller |
Receiver | Hobby King 2.4Ghz Receiver 6Ch V2 |
Remote Control | Hobby King 2.4Ghz 6Ch Tx and Rx V2 |
Battery | Zippy Flightmax 1300mAh 3S1P 20C |
(OTHER:) |
Problems:
- The three screws holding the bot and the skids in place were difficult to remove because of the threaded standoff in the middle
- Exposed space above and below the weapon ring can be exploited/allows small enemies to evade the weapon
- The motor controller had loose connections
- Weapon ring prone to slipping off the burnt down rubber bearing ring
- Wheels were prone to becoming loose and slipping off the drive motor shaft
Good aspects:
- Can attack from all sides
- Has no exposed, non-attacking sides
- Can drive right side up and up-side-down
- Most Parts are easy to remove/repair/replace
- Relatively difficult to damage severely
Changes/Improvements:
- Change the rubber rings to plastic
- Find a better way to secure the wheels to the motors
- Make the robot thinner
- Make the weapon closer to the ground, and cover more of the robot
- Find a better way to hold the robot together
See also
Notes:
HE WAS #1
Name inspired by an episode of SpongeBob Squarepants
Built by Aman More, Cory Stine, and Dustin Sloan