Guillotini

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Revision as of 13:40, 14 May 2021 by Acollier31 (talk | contribs)
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Guillotini
Year of Creation 2020-2021
Versions
Current Version 1.0
Update Year 2020-2021
Wins/Losses 2/1
Information and Statistics
Weight Class 2lb
Weapon Class Horizontal Spinner
Combined Wins/Losses 2/1
Weapon Speed (number) RPM

(insert summary here)


Competitions

2lb Competition 2021

  • Results:
    • Single Elimination:
      • [WIN vs Dizzi]
        • weapon spun up!!!
        • then the belt slid off D:
        • was able to get in one good hit which we believed messed up Dizzi's weapon system.
        • won through judge decision based off of aggressiveness
      • [WIN vs Wonki]
        • weapon hates us :(
        • won by being aggressive
      • [LOSS vs Largetoni]
        • weapon didn't spin up
        • bruh we were sitting ducks
        • did the best we could, Largetoni got off several good hits
        • Largetoni cracked the bottom chassis
        • kept fighting
        • one last hit and the Guillotini's battery popped out, judges terminated battle

Version

botName V1.0

Created by: (Names of Builders/Group Members of aforementioned version of bot)

Drive Motors 22mm DC gearmotor
Drive Motor Controllers Scorpion Mini Electronic Speed Control
Weapon Motor weapon motor name
Weapon Motor Controllers weapon esc name
Receiver Hobby King 2.4Ghz Receiver 6Ch V2
Remote Control Hobby King 2.4Ghz 6Ch Tx and Rx V2
Battery Turnigy Nano-Tech 1000mAh 3s 45~90c LiPo Pack
OTHER:

Problems

  • Weapon belt would slide off the weapon pulley when spun up to high speeds
  • Weapon system was unreliable and would occasionally not spin up at all
  • Wheels purchased were too small and had to be made bigger by wrapping rubber tape around its circumference
  • Wheels and weapon motor took up more space than expected, requiring the chassis to be sanded down to make them barely fit.
  • Outer edges of the drive wheel holes and the internal wires would rub against the wheels, causing differences in friction between the wheels and making the robot not drive straight.

Good aspects

  • Was just underweight without having to do any extra weight-reduction procedures
  • Drive system was functioning all three matches
  • The wheels were well protected

Changes/Improvements

  • The weapon pulley design would have to be changed to prevent the weapon belt from slipping
  • The entire bot should be a little bit bigger to help everything fit better
  • The clearance on the drive wheel holes should be larger
  • The wall thickness could be lower but with a higher infill
  • The cutout patterns on the sides should be printed thicker or made bigger to increase structural strength

Notes:

Random joke: our weapon

Also: i tried to copy/paste the Bee Movie script but it wouldn't work

named after an execution weapon because it was metal as frick

proceeded to fail to chop up any bots

feelsbadman

Created by: Michael C. (mentor), Sam H., Lucas L., Brian N., Alex C., Aislinn A.